Boeing 737-300
Safety Rating
8/10Total Incidents
37
Total Fatalities
726
Incident History
Serve Air
The airplane departed Kinshasa-N'Djili Airport on a cargo flight to Lubumbashi, carrying five crew members and one passenger. Following an uneventful flight, the crew was cleared to descend and to land at Lubumbashi-Luano Airport. After landing on runway 07, the crew started the braking procedure. At a speed of 80 knots, the aircraft deviated to the left. It veered off runway and while contacting soft ground, the nose gear collapsed. The airplane came to rest in a grassy area along the left shoulder of the runway after a course of about 200 metres. All six occupants evacuated safely and the aircraft was damaged beyond repair.
Tri-MG Intra Asia Airlines
The aircraft was performing a cargo flight from Timika, carrying five crew members and a load of various goods including constructioin materials. Upon landing on runway 15, the airplane bounced twice. It went out of control and veered off runway to the left. While contacting soft ground, both main landing gear were torn off and the aircraft slid for few dozen metres before coming to rest. All five crew members evacuated safely while the aircraft was damaged beyond repair.
Sriwijaya Air
On 31 May 2017, a Boeing 737-300 aircraft registration PK-CJC was being operated by PT. Sriwijaya Air as a scheduled passenger flight from Hasanuddin Airport (WAHH), Makassar, South Sulawesi to Rendani Airport (WAUU), Manokwari, West Papua, with one transit stop at Domine Eduard Osok Airport (WASS) Sorong, West Papua. The flight was uneventful since the first departure from Makassar until commencing the approach at Manokwari. At 0815 LT (2315 UTC), the aircraft departed Sorong to Manokwari. On board in the flight were two pilots, four flight attendants and 146 passengers. On this flight, the Second in Command (SIC) acted as Pilot Flying (PF) and the Pilot in Command (PIC) acted as Pilot Monitoring (PM). At 2331 UTC, the pilot made first contact to Rendani Tower controller and informed that the aircraft was descending from FL 230 (altitude 23,000 feet) and requested the weather information. The Rendani Tower controller informed to the pilot that the wind was calm, ground visibility 6 km, cloud FEW CB 1,400 feet, temperature and dew point 26/25°C. At 2336 UTC, Rendani Tower controller instructed to the pilot to descend to 11,000 feet and to report when on Visual Meteorological Condition (VMC). At 2338 UTC, the pilot informed that they were on VMC condition and passed altitude 13,000 feet while position was 32 Nm from ZQ NDB (Non-Directional Beacon). Rendani Tower controller instructed to fly maintain on visual condition, fly via overhead, descend to circuit altitude, join right downwind runway 35, and to report when overhead Manokwari. At 2344 UTC, the pilot reported that the aircraft was over Manokwari and Rendani Tower controller informed to the pilot that the visibility changed to 5 km. Two minutes later Rendani Tower controller instructed to the pilot to continue approach and to report on right base runway 35. At 2349 UTC, at approximately 600 feet, the PIC as PM took over control by called “I have control” and the SIC replied “You have control”. A few seconds later the pilot reported that the aircraft was on final runway 35, and Rendani Tower controller instructed to the pilot to report when the runway 35 insight. The pilot immediately replied that the runway was in sight and acknowledged by Rendani Tower controller who then issued landing clearance with additional information that the wind was calm and the runway condition wet. At approximately 550 feet, the PIC instructed the SIC turn on the wiper and reconfirmed to SIC that the runway was in sight. Between altitude 500 feet to 200 feet, the EGPWS aural warnings “Sink Rate” and “Pull Up” sounded. At 2350 UTC, the aircraft touched down and rolled on runway 35. The spoiler deployed and the pilot activated the thrust reversers. The crew did not feel significant deceleration. The aircraft stopped at approximate 20 meters from the end of runway pavement. After the aircraft stopped, the PIC commanded “Evacuate” through the Passenger Address (PA) system. The Rendani Tower Controller saw that the aircraft was overrun and activated the crash bell then informed the Airport Rescue and Fire Fighting (ARFF) that there was an aircraft overrun after landing on runway 35. All the flight crew and passengers evacuated the aircraft and transported to the terminal building safely.
Peruvian Airlines
The aircraft departed Lima-Jorge Chavez Airport on a 20-minute flight to Jauja, carrying 142 passengers and 7 seven crew members. The approach to Jauja-Francisco Carlé was uneventful and completed in good weather conditions. Two seconds after the nose gear touched down on runway 31, the crew activated the reverse systems when he felt strong vibrations and oscillations. The aircraft started to bounce and became uncontrollable. The right main gear collapsed then the aircraft veered off runway to the right, lost its right engine and came to rest in a grassy area, bursting into flames. All 149 occupants evacuated safely and the aircraft was totally destroyed by fire.
Trigana Air Service
On 13 September 2016, a Boeing 737-300 Freighter, registered PK-YSY was being operated by PT. Trigana Air Service on a scheduled cargo flight from Sentani Airport, Jayapura (WAJJ) to Wamena Airport, Wamena (WAVV), Papua, Indonesia. Approximately 2130 UTC, during the flight preparation, the pilot received weather information which stated that on the right base runway 15 of Wamena Airport, on the area of Mount Pikei, low cloud was observed with the cloud base was increasing from 200 to 1000 feet and the visibility was 3 km. At 2145 UTC, the aircraft departed Sentani Airport with flight number IL 7321 and cruised at altitude 18,000 feet. On board the aircraft was two pilots and one Flight Operation Officer (FOO) acted as loadmaster. The aircraft carried 14,913 kg of cargo. The Pilot in Command (PIC) acted as Pilot Flying (PF) while the Second in Command (SIC) acted as Pilot Monitoring (PM). There was no reported or recorded aircraft system abnormality during the flight until the time of occurrence. After passing point MALIO, the aircraft started to descend. The pilot observed the weather met the criteria of Visual Meteorological Condition (VMC). The pilots able to identify another Trigana flight from Sentani to Wamena in front of them. While passing altitude 13,500 feet, approximately over PASS VALLEY, the Wamena Tower controller instructed the pilot to report position over JIWIKA. When the aircraft position was over point JIWIKA, the Wamena Tower controller informed to the pilot that the flight was on sequence number three for landing and instructed the pilot to make orbit over point X, which located at 8 Nm from runway 15. The pilot made two orbits over Point X to make adequate separation with the aircraft ahead prior to received approach clearance. About 7,000 feet (about 2,000 feet above airport elevation), the pilot could not identify visual checkpoint mount PIKEI and attempted to identify a church which was a check point of right base runway 15. The pilot felt that the aircraft position was on right side of runway centerline. About 6,200 feet (about 1,000 feet above airport elevation), the PF reduced the rate of descend and continued the approach. The PM informed to the PF that runway was not in sight and advised to go around. The PF was confident that the aircraft could be landed safely as the aircraft ahead had landed. Approximately 5,600 feet altitude (about 500 feet above airport elevation) and about 2 Nm from runway threshold the PF was able to see the runway and increased the rate of descend. The pilot noticed that the Enhanced Ground Proximity Warning System (EGPWS) aural warning “SINK RATE” active and the PF reduced the rate of descend. While the aircraft passing threshold, the pilot felt the aircraft sunk and touched down at approximately 125 meters from the beginning runway 15. The Flight Data Recorder recorded the vertical acceleration was 3.25 g on touchdown at 2230 UTC. Both of main landings gear collapsed. The left main landing gear detached and found on runway. The engine and lower fuselage contacted to the runway surface. The aircraft veer to the right and stopped approximately 1,890 meters from the beginning of the runway 15. No one was injured on this occurrence and the aircraft had substantially damage. Both pilots and the load master evacuated the aircraft via the forward left main cargo door used a rope.
Southwest Airlines
On December 15, 2015, at 5:23pm central standard time (CST), Southwest Airlines flight 31, a Boeing 737-300, N649SW, exited the taxiway while taxing to the gate and came to rest in a ditch at the Nashville International Airport (BNA), Nashville, Tennessee. Nine of the 138 passengers and crew onboard received minor injuries during the evacuation and the airplane was substantially damaged. The airplane was operating under the provisions of 14 Code of Federal Regulations Part 121 as a regularly scheduled passenger flight from William P. Hobby Airport (HOU), Houston, Texas. Weather was not a factor, light conditions were dark just after sunset. The airplane landed normally on runway 20R and exited at taxiway B2. The flight crew received and understood the taxi instructions to their assigned gate. As the crew proceeded along taxiway T3, the flight crew had difficulty locating taxiway T4 as the area was dark, and there was glare from the terminal lights ahead. The crew maneuvered the airplane along T3 and onto T4, and then turned back to the right on a general heading consistent with heading across the ramp toward the assigned gate. The flight crew could not see T4 or the grassy area because the taxiway lights were off and the glare from the terminal lights. As a result, the airplane left the pavement and came to rest in a drainage ditch resulting in substantial damage to airplane. The cabin crew initially attempted to keep the passengers seated, but after being unable to contact the flight crew due to the loud alarm on the flight deck, the cabin crew properly initiated and conducted an evacuation. As a result of past complaints regarding the brightness of the green taxiway centerline lights on taxiways H, J, L and T-6, BNA tower controllers routinely turned off the taxiway centerline lighting. Although the facility had not received any requests on the day of the accident, about 30 minutes prior to the event the tower controller in charge (CIC) turned off the centerline lights as a matter of routine. In doing so, the CIC inadvertently turned off the "TWY J & Apron 2" selector, which included the taxiway lights in the vicinity of the excursion. The airfield lighting panel screensaver feature prevented the tower controllers from having an immediate visual reference to the status of the airfield lighting.
Magnicharters
The aircraft departed Cancún on a regular schedule flight to Mexico City, carrying 139 passengers and five crew members. The flight was uneventful. Following an unstabilized approach, the aircraft landed on runway 05L at an excessive speed. After touchdown, severe vibrations occurred when the left main gear collapsed after a course of 1,097 metres. The airplane slid for 980 metres before coming to rest. All 144 occupants evacuated safely and the aircraft was damaged beyond repair.
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Safety Profile
Reliability
Reliable
This rating is based on historical incident data and may not reflect current operational safety.
